Many thanks to everyone who has contributed so far.
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Guests and others. Dont just read this! Please contribute. There is a lot of data and info in this forum from every level of ownership, ability and experience.
Best regards.
Ant
Hi Ant, just gathering it all together, and as follows:-
Bavaria 36 2002
1a leaking port light seal - fixed with a smear of Vaseline.
1c all stanchion bases re-sealed, and hands cut off any visitor that uses the stanchions to haul themselves onboard.
1i leaking pump diaphragm
1o leaking F.W. Pump filter (two parts don't fit together very well)
2b no actual problem, but changed after 9yrs and found perfect
2e raw water pump seal small leak and was changed.
2i exhaust silencer s.s. Ends corroded - changed for all plastic £58 silencer almost one year ago and all ok now.
2j no leakage, but rudder bearing changed after heavy vibrations which now stopped.
3a original starter battery not holding charge and changed after 14 years.
Extra point 3k engine starter push button collapsed and a new starter button fitted which works ok.
4h Lack of diesel - forgot to open fuel valve, but it allowed diesel fuel to pass through but not enough for much more than 2000rpm but for at least three hours
5a saildrive waterway partially blocked by mussel shells
5d heat exchanger seawater inlet end blocked by previous owners pump impeller blades and mussel shells
(5k - should this read Heat exchanger leaks FROM salt water side to FW (blows water out of header tank)
5l see 5f poor design of raw water filter allowed mussel shells to pass thro filter and pump to lodge in entrance to heat exchanger.
8d saildrive difficult to disengage - suspect problem with morse control.
8g milky oil in sail drive at 1st change after buying boat in 2010. Shaft seal changed and no further problem.
9e alternator not charging after work done on 2b where yard mechanic incorrectly connected alternator wires to wrong terminals.
9i fridge not cooling 1. due poor insulation and later 2. Due to loss of refrigerant where pipe chafed against woodwork. Insulation improved but still work in progress, and recharged refrigerant gas and re-routed the pipe to avoid chafe.
9o steaming and tricolour lights not lighting due to corrosion on original ordinary copper wire cabling.
9q water tank level gauge fails. Happened six years ago, and just ignored.
10f two new cupboard door push button latches fitted where the originals failed.
Plenty more stuff for next set of survey questions.
Regards
Salty